Testing v1 0
Version 6 (Jeremy Wright, 01/02/2013 08:35 pm)
| 1 | 1 | Jeremy Wright | h1. Testing v1.0 |
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| 2 | 1 | Jeremy Wright | |
| 3 | 1 | Jeremy Wright | {{toc}} |
| 4 | 1 | Jeremy Wright | |
| 5 | 2 | Jeremy Wright | The testing was done in three main phases, with the first two progressing in parallel: |
| 6 | 1 | Jeremy Wright | # The mechanical system was tested as a stand-alone unit. |
| 7 | 1 | Jeremy Wright | # The Data Acquisition (DAQ) system was tested as a stand-alone unit. |
| 8 | 1 | Jeremy Wright | # The mechanical and DAQ systems were integrated and then tested. |
| 9 | 1 | Jeremy Wright | |
| 10 | 1 | Jeremy Wright | h2. Mechanical System Testing |
| 11 | 1 | Jeremy Wright | |
| 12 | 3 | Jeremy Wright | Below are several videos taken during the initial mechanical tests of the test stand by J. Simmons at "Dayton Diode":http://www.daytondiode.org/ in Dayton, Ohio. |
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| 14 | 1 | Jeremy Wright | {{youtube(Qso1bQiXL1M)}} |
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| 16 | 4 | Jeremy Wright | {{youtube(fqcyojvl8nQ)}} |
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| 18 | 4 | Jeremy Wright | {{youtube(1ukNd91BeW0)}} |
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| 20 | 4 | Jeremy Wright | {{youtube(sMVKv2a9Lb4)}} |
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| 22 | 4 | Jeremy Wright | {{youtube(WLG6kW-XHB8)}} |
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| 24 | 1 | Jeremy Wright | h2. DAQ System Testing |
| 25 | 1 | Jeremy Wright | |
| 26 | 3 | Jeremy Wright | During DAQ System testing, it was discovered that the data collection rate of the system was much too low, being around 15 samples per second. This is due to the fact that the MAX31855 thermocouple amplifier takes between 70 and 100 milliseconds to convert its reading. |
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| 28 | 1 | Jeremy Wright | h2. Integrated Testing |
| 29 | 3 | Jeremy Wright | |
| 30 | 3 | Jeremy Wright | During the integrated testing, 2 more flaws were discovered in the design. |
| 31 | 3 | Jeremy Wright | |
| 32 | 3 | Jeremy Wright | # The drawer guide used as the linear rail for the motor mount tended to foul within 30 to 50 test firings due to the fact the ball bearings were exposed to the motor exhaust particulates. Figure 1 shows the fouling. |
| 33 | 3 | Jeremy Wright | # The Force Sensing Resistor (FSR) that was specified for the test stand was not capable of registering anything higher than 10 Newtons of force. This puts some of the higher thrust motors beyond the range that the FSR can measure. |
| 34 | 3 | Jeremy Wright | |
| 35 | 3 | Jeremy Wright | *Figure 1 - Fouling of the Drawer Guide's Bearings By Exhaust Particulates* |
| 36 | 5 | Jeremy Wright | !Drawer_Guide_Fouling.png! |
| 37 | 3 | Jeremy Wright | |
| 38 | 6 | Jeremy Wright | It was also realized before the first test firing that the motor mount contact pad would have to be added. This was to ensure that the thrust of the motor was spread over the entire sensing surface of the FSR and not beyond into the substrate border. |
| 39 | 6 | Jeremy Wright | |
| 40 | 3 | Jeremy Wright | Below are several videos taken during the integration tests of the test stand by J. Simmons and Jeremy Wright at "Club Cyberia":http://www.clubcyberia.org/ in Indianapolis, Indiana. |
| 41 | 3 | Jeremy Wright | |
| 42 | 3 | Jeremy Wright | TODO: Add videos of integration testing |